Once that is done...on to mucking with the brakes. And, oh, yeah...got new throttle and choke cables. Thinking replacing them is going to be a goat rodeo...a lot easier when the lump is out of the car, but not there yet, so...
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Was just spitballing (poking a stick in the cage?). Have the intake down to the head flanges all apart...finding all sorts of DPO happiness (like no nuts on the 2 bottom studs holding both of the carbs on the adapter plate to the secondary throttle assembly), copious amounts of RTV squeezed out of joints, thackery washers torqued down tight, idle trim screws set vastly different between front and rear carbs, 2 different tapered needles (I have their mates in a box of spare parts...) in the pistons...So...back to 'stock' (except for the lack of secondary throttles) and set up per the book.
Have cleaned up the threads on the pile of 5/16x24 nuts, ran a die down all the studs to clean up those parts, have a stack of new split and flat washers to use where needed, new thackery washers, new gaskets, new diaphragms, new o-rings, new floats, new needle valve, a gallon can of carb dip and a couple parts brushes. Time to dig in, clean up, rebuild, and reinstall...
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Hope I'm not starting a religious war here...but probably talking heresy regarding the braking system in US JPS 142.
IMHO, a 1500 lb car with 120(?) HP in this day and age...it's over-engineered a bit to put double boosters in the circuit, aside from the piping complexity. Like...I'm not going to autocross, not doing hot laps at Jersey Motorsport...I'm going down to Dunkies for my morning caffeine fix, driving the SO to Second Beach in Newport, or carving some corners in the backroads of Bristol County MA. So...the unworking boosters, assorted vacuum lines, and other items are coming out. That's a given; while waiting for the various bits and pieces of interior stuff to come back...figure it's time to sort the brake system out (along with overhauling/cleaning up the pedal assembly, replacing the original clutch and accelerator cables, etc.) before assuming the Lotus Position and cleaning up the 'back of the dash' from 50 years of unconcerned mucking about back there. And, to be honest...the S2 got away just fine with an unboosted system, and it's within a couple hundred pounds of its later sibling.
So...what to do?
As a starting point (the rear cylinders were replaced recently, along with pads, so, assuming the job was done correctly, going to leave sleeping dogs lie after inspecting)
After this?
1. Open the taps and drain the system, disposing of the existing fluid.
2. Disconnect and remove the vacuum units, patching the holes in the fiberglass, and repainting the side wall on that side (truck bed liner paint, minus the grit which I filter out is my preferred finish for the engine room and wheel arches).
3. Remove the flex hoses from the front and rear. They are original...and will be replaced with armored hose replacements.
4. Rebuild front calipers with stainless pistons (have a set left over from my own stock), paint calipers, reload with fresh pads.
5. I have new disks I was going to put on 693R but never got a round tuit...so, might as well use them here.
6. Remove the MC. It's a girling unit, looks like the original...but who knows? Mucking through the extensive records I have, don't see any indication that it was replaced along the line, but, pretty sure not every bit was recorded in the POs OCD record keeping.
Now...it's all in bits...where to go from here?
There are a lot of thoughts about which direction to travel; let's face it, some of the parts, while made by Girling, were made to Lotus' specs and are not current production. There are docs on the manuals site (either Dan's or my mirror) that go into gory detail about decisions: Nissan/Tilton/Spitfire/you name it. Some bits are still available, some not. It seems at this point it will be pretty much narrowed down to either a Tilton or the Spit master...(in my mind...).
Removing the boosters means that the bore size of the master and travel will need to be somewhat different. In the S2, for instance, the .70 bore took care of the fronts, and the stepped-down bore (don't recall offhand the size) at the rear of the cylinder took care of the rears. Fair enough. The replacements today have a constant bore in various sizes...Tilton, being a universal fittment, is available in multiple bores: 5/8, .70, .75, etc. Generally, the larger the bore, the less travel to fully engage...the smaller the bore, the more travel. Basic fluid dynamics, right? Coming up with a compromise between feel, travel of the pedal, and force applied becomes a question to answer.
Aside from the physics of fluid travel, pipe bending and terminating, etc., and accounting for the removal of the boosters (which modulated the feel of the brakes and balanced the force needed), I'm in the range of thinking that moving from an assisted to a non-assisted system is pointing towards ensuring that the front-rear balance is maintained properly...which means that
1. the fluid force applied to the rear will have to be moderated by a proportioning valve to make up for the larger MC bore feeding them and
2. using the same bore size as the unboosted cars used for the fronts will provide both the right travel as well as fluid force for the calipers (which are the same on the TC as were on the S2).
Am I off here? For the record, I'm basing this on reading Aaron Hines' work done in the early aughts, as well as Dave Maugham's document on his changes...and some of the Lotus West material (thank goodness for the archive, right?).
Where I'm leaning towards (yeah, using a heavy iron speed shop...) is:
1. Tilton 74-700U master cylinder (https://www.jegs.com/i/Tilton/454/74-700U/10002/-1) with reservoir remote mounted up on front trunk bulkhead and front line direct connected to fluid T on front of frame, removing the back-and-forth piping to the removed booster. That means the PDWV goes away. Simplifying the piping means fewer points of failure, which the valve was meant to monitor. (I realize this may result in some comments, so be it...I'm open to reasoned arguments to keep or not)
2. Jegs Proportioning Valve model 63020 (https://www.jegs.com/i/JEGS/555/63020/10002/-1) in place of the rear booster (in essence)
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I'll just let the photos tell the story. Didn't use foam padding, just flexible leatherette from the local sewing supplies store. Dipped into my store of aircraft upholstery supplies for the cement, which is a high-solids, high-tack cement used to finish aircraft interior panels. Seam was tightly sewn to the edge as close as possible then trimmed carefully.
Key is to let the cement flash off completely, and use a sharp razor knife to point the leatherette as you go around curves or inside corners. It's fiddly (no doubt the ladies in the trim shop at Hethel were a lot faster), but if you take your time, it all works out well enough.
Fiberglass base was stripped of all the old cover (which I used as a general pattern...), foam, then sanded lightly to remove the old cement. Luckily it was in good shape and ready to receive the cement. I did one panel at a time, starting with the front, and stretched the leatherette as it was smoothed down on the base after the cement flashed off.
Think it came out OK; it only has one attachment screw in the front face that goes into the switch mechanism metal flange. Thinking, for sturdiness sake (and to give the switch gear a little more stability), I may put two holes in the bottom that align with the base of the dash, and use some #6 black trim screws up from the bottom, and build a short flange out of aluminum and do the same for the top. We'll see when I get back to MA and keep working on the car...
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At the base....you will have (deteriorated) nylon 'top hat' bushings IN the base of the lever. The shoulder bolt will be inserted from the driver side through the base (there's a welded stop to prevent it from turning...when you tighten or loosen the nyloc nut on the other end. Under the nyloc nut is a washer. The whole assembly is (assuming you have a TC or an upgraded S2 that uses the TC parts) is as you see it in the photo above.
You will have to get your forearm IN all the way and do by feel. Yes, things COULD drop into the frame, but a magnet stick works wonders to pick up pieces that may disappear. Just take your time (thinking the factory had a select group of assemblers who either had very thin forearms...or built the whole thing out of the car and pushed it into the frame before dropping the engine in...I've done it both ways...); I've found that it takes about a half hour and much contortions (helps if you pull the seats so you can kneel on the floor) but taking it a step at a time works just fine.
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Got a question:
"That sounds like a major effort for the Euro tail lights! I wonder if just buying Euro lamps wouldn't have been cheaper..."
My response:
They were euro taillights off a canadian body I bought. I just restored them (new ones, last I checked were over 1K USD for a pair, if you can find them); I like the fiddly work of hands-on renovation of the appliances. Especially when it works when you're finished.
Checked my receipts and the rechrome back then cost me 150 for each, and the lenses were 100 or so each from Banks. Had all the internals/springs/etc, so it was just a matter of my hand work to finish them.
Federal cars have a relay box under the dash so that one filament in the solid red lens tail light can work as both the brake and the directional; when your foot is on the brake, and you engage the directional, it allows the same filament to blink while still keeping the other filament on the other side steady on as the brake is applied. That, and the regs at the time, stated that rear directionals had to be red. It's 2022...no one cares about a 50 year old car as to whether the directionals are the right color...just that they work.
Just adding the Green/purple wire from the brake switch direct to the stop lights (tying back the GP that goes to the DB10 relay box) and moving the green/white and green/red to the top filaments is a simple job.
Just replaced the reverse with LEDs. I usually change out the flasher anyway to an electronic unit that will work with either incandescent or LED...constant flash rate no matter the voltage, and quiet. So, if I wanted to put in LED replacements, it's an easy swap. Anything to reduce the current draw on these old harnesses (I did all the position and landing/taxi lights in my plane under approval with LEDs...they're brighter, and the current draw according to the meter in my plane panel is almost negligible versus the incandescents that were in there before.)
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Euro taillights polished and ready to install. While still ruminating about what to do about the motor...working on other items of interest.
The TC wiring loom for federal cars (versus the S2, which ran a wire forward from the brake switch to the DB10 and left the other brake light wire in place in the loom) does not mirror the S2 arrangement, which made it easy to install the euro taillights after I painted 693R in '08.
So..ordered up some proper color wire (and bullets, etc) from Brit Wiring in the right size and will add the wire into the back end at some point, and wire the car as per the euro wiring chart for the blinkers/stop/hazard/running lights.
For the record...the bases were stripped and replated, new sponge gasket under the lenses, bases retapped for 6/32 to attach the lenses (using stainless hardware), mounting threads cleaned up (1/4x20) and have new base gaskets. All the light sockets were chromed at the same time, but, re-flowed the solder on the light contact bases, new bullets (crimped and soldered) for the light leads, and the reverse light assemblies rebuilt and connectors polished....and LED festoon bulbs used.
Was going to put these on the second S2 that I had thought I was going to build...but...ran out of steam with some medical issues in '09 and never got to it, selling the frame and second body off as time went on.
Thinking of offering the steering wheel I pulled out. It's in perfect shape...but only good for a TC, since 1) I have no idea who manufactured it or where to get the horn button fixings...and 2) that's the model it came out of.
And...spent some time with a buffer, chrome polish, and went after the bumpers. They are 40 something years old...but only a couple scratches and rub marks, but certainly are not something to be ashamed of. Considering the cost to strip, buff, replate...they'll do.
Packed up the seat with the torn seams on the bolster and a piece of carpet (and measurements for the floor on both sides)...and drove to the next town over to the only auto upholstery shop in the Fall River area. Closed due to a positive covid test until April. Sigh. Oh well, the other seat is ok. No rush on any of this, but was thinking of getting ahead of some things. Hope he's ok...and will revisit later.
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Fiddly is NOT the word. The replacements are for a larger diameter column so...somehow you have to build the column up so that you can clamp it down tightly. First problem. I solved it with a couple rings of large adhesive heat shrink (I use it when I make high-power RF coax terminations on the end of heliax) which makes up most of the difference. I then carefully, with an extremely sharp bit, drilled a pilot hole 180 degrees from the clamp screw, and once the proper diameter was achieved with the heat shrink, and the clamp was tightened down fully, screwed a short stainless #6 sheet metal screw in so that the point pierced the heat shrink and bit into the column. It's tight.
Second problem...the quality of the ostensibly 'Lucas' replacement parts is questionable...I rang out all the leads and except for the horn button, everything was copacetic. Carefully disassembled the new rront plate (which has a different shape than the original... removed the stalk (yeah, there are a bunch of springs, wipers, one ball...I did it upside down in a tupperware container and caught everything), removed the offending stalk from both (the horn worked on the old switch plate...) and thank goodness the old stalk worked in the new switch housing...and the horn button worked, too...reassembled the new switch back end with the old plate (there is a screw hole for the column cover; the new front plate is a different shape, so there would have been no place to attach the cover...) Other issue is that the new turn cancel cam is deeper than the old...so, while reassembling, used the old nylon cam instead of the new one.
third issue: the plug at the end of the wire bundle for the switch is different. So...cut off the old molex (I don't have a pin removal tool for the large .092 pins...only the smaller .062...my bad...) with enough wire to splice onto the new wires. Soldered like colors to like color, shrink tube over the splice, and tested before wrapping with loom tape. Everything works as it should.
Put it all together on the column (with the lock screw...), plugged everything in, reattached the ground on the battery...turned the key...can flash the lights, hi/lo beam, turn sigs, horn, wipers, squirters...
Now, to finish with the leatherette cover for the column cover and put it all back with the OEM steering wheel.
I would hate to think about how much it would have cost to have someone do it for me. Lots of fiddling, fitting, and thinking outside the box...
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Figured during lunch hour...would start to do a few things on the interior of JPS 142 while musing about what to do about the engine...drop and refresh or fiddle around more with her...anyway...stripped out the seats. The passenger side is just fine; driver side seams are torn. Thinking to just see if an upholstery shop can make up a pair (they're mirror images) of the bolsters and replace. I know Europa Engineering ostensibly lists seat cover kits for 95 UKP each...maybe they would just make up bolsters? Anyway...will switch seats for now (and move the sensor and pad to the driver seat when I install on the passenger side...).
Stripped out the nasty insulation from the floor of the driver side, shop vacuumed the carpet vigorously. Came up with some loose change with 70s and 80s dates. Like rummaging through the sofa, right? Will put down dynamat on the floor on that side to deaden the drumming. Looking at the pedal assembly...looks like someone "adjusted" the clutch pedal side to side angle...will take that out at some point and put it back where it belongs...and took out the aftermarket steering wheel. I think the original one looks a lot nicer. Will have to take it off anyway again, and drop the column; the clamp holding the stalk assembly is broken...and RD was able to supply a replacement. BUT, the right side washer stalk is riveted onto the plate...will attempt to CAREFULLY drill out the rivets and attach with machine screws...if not, will just pick up another stalk and be done with it...and probably freshen up the paint on the column and mount. Vinyl covering the stalk cover is beyond use; made a pattern of the old vinyl leaving a generous edge for gluing purposes...my SO is going to stitch up the pieces, and will recover the fiberglass with fresh 'leatherette'.
And...fiddling around with the center console; I think I'll just leave it original. If I want to add gauges, MOSS sells a radio delete plate with 3 small gauge holes in it that I can use and delete the radio (or mount elsewhere...or not...just replace with an amp and leads to feed from my i-device. Like my selection of tunes better than what's on broadcast anyway...And it will keep the interior as stock as possible.
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A bit of 'fettling' that needs be done. Getting it started and running would be a start. Right now, it barely starts (with a lot of cranking), spits gas out of the carbs, pops and fluffs...and has a big flatspot from idle to full accelerator pedal down.
Replaced plugs (removed ones are black and sooty...). Thinking of investigating the ignition timing next. And getting the ass end up in the air to get the left tank out and on it's way to Moyer in PA to be sealed.
At this rate, I don't forsee her being ready for the road for a while.
UPDATE:
Maybe it would help if the dizzy was timed properly. Just for S&Gs...reached under the carbs (the airbox is off...), and found that the distributor lock plate was not tightened down. Now, Who the F would fiddle with a dizzy and not lock it down when they were done. Not going to blame the PO, since he was a Porsche/Audi man, but, geez, people.
Now, have to figure out where TDC is and get the distributor lined up so I can at least time it. Thinking that was the issue all along with getting it running. We'll see.
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